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CNC / Re: It's new to me
« Last post by ddmckee54 on April 25, 2026, 01:46:49 AM »Sometimes I'm just not as smart as I think I am...
I got the Z axis leadnut plate drilled and tapped in the appropriate places, I also managed to snap off my M3 spiral tap in the process. While running the tap in far enough to be sure all the chips were cleared out of the threads, I ran the spiral tap through the plate. While trying to start the tap back into the hole I managed to get it started crooked, and snapped it off. Fortunately there was plenty of the broken tap sticking out of the back of the plate that I could grab onto and thread it out. I had one other M3 tap, a 4 flute tap, and wanted to chase the threads - but I didn't want a repeat of the previous disaster. So I drilled a clearance hole in a piece scrap plastic and made a simple M3 tap guide. I used that to chase the threads, and also to tap the one remaining M3 hole on the Z axis leadnut plate.
I then set about assembling the anti-backlash leadnut, and getting it adjusted. The process I used to assemble/adjust the Y axis leadnut is identical for all three leadnuts; the only thing that varies is the shape of the leadnut plate. So... Onto installing the leadnut into the spindle slide.
Anddddd... it doesn't fit. Oh, it fits into the pocket alright, it's just that ALL of the leadnut doesn't fit into the pocket. The top of the leadnut plate is still 1-2mm proud of the surface and it should be flush.
The cause of this evil deed? When assembling the Y axis leadnut I discovered that when using the M3x35mm bolts as originally designed, if the two halves of the leadnut weren't clocked properly, I either couldn't assemble the leadnut halves or the nylock adjusting nuts wouldn't lock. My leadscrews are T8 2 start screws, with a 4mm pitch. With the Y axis leadnut, the only way the M3x35mm screws would work was if the 2 halves of the leadnut were threaded so close together that I couldn't remove the backlash in the threads. Clocking the 2nd half of the leadnut to the other start moves that half by 2mm, which allowed me to adjust out the backlash. Unfortunately, that also moved the adjusting nut by 2mm, far enough that the nylon locking ring wasn't doing its' job. I had M3x40mm screws, which solved that problem. What it didn't solve was that the pocket the leadnut fits into on the spindle slide had 2mm of clearance - when using an M3x35mm screw.
Sometimes I'm just not as smart as I think I am.
I got the Z axis leadnut plate drilled and tapped in the appropriate places, I also managed to snap off my M3 spiral tap in the process. While running the tap in far enough to be sure all the chips were cleared out of the threads, I ran the spiral tap through the plate. While trying to start the tap back into the hole I managed to get it started crooked, and snapped it off. Fortunately there was plenty of the broken tap sticking out of the back of the plate that I could grab onto and thread it out. I had one other M3 tap, a 4 flute tap, and wanted to chase the threads - but I didn't want a repeat of the previous disaster. So I drilled a clearance hole in a piece scrap plastic and made a simple M3 tap guide. I used that to chase the threads, and also to tap the one remaining M3 hole on the Z axis leadnut plate.
I then set about assembling the anti-backlash leadnut, and getting it adjusted. The process I used to assemble/adjust the Y axis leadnut is identical for all three leadnuts; the only thing that varies is the shape of the leadnut plate. So... Onto installing the leadnut into the spindle slide.
Anddddd... it doesn't fit. Oh, it fits into the pocket alright, it's just that ALL of the leadnut doesn't fit into the pocket. The top of the leadnut plate is still 1-2mm proud of the surface and it should be flush.
The cause of this evil deed? When assembling the Y axis leadnut I discovered that when using the M3x35mm bolts as originally designed, if the two halves of the leadnut weren't clocked properly, I either couldn't assemble the leadnut halves or the nylock adjusting nuts wouldn't lock. My leadscrews are T8 2 start screws, with a 4mm pitch. With the Y axis leadnut, the only way the M3x35mm screws would work was if the 2 halves of the leadnut were threaded so close together that I couldn't remove the backlash in the threads. Clocking the 2nd half of the leadnut to the other start moves that half by 2mm, which allowed me to adjust out the backlash. Unfortunately, that also moved the adjusting nut by 2mm, far enough that the nylon locking ring wasn't doing its' job. I had M3x40mm screws, which solved that problem. What it didn't solve was that the pocket the leadnut fits into on the spindle slide had 2mm of clearance - when using an M3x35mm screw.
Sometimes I'm just not as smart as I think I am.
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